It was a challenge to get the planks to snuggle up to each other, especially at the bow and stern. I broke a lot of wire. I started in the middle and worked to the ends. The first pass I got them in the ball park and then tightened again from middle to ends until I broke the wire. I replaced it and repeated the process until the ends came together. For the final 12 inches, I had to get a friend to help squeezed the planks together and I handled the wire.
In the next step, epoxy is put into the seams. Here, I had another of my many opportunities for improvement. I made up the mix of epoxy and Cab O Sil too thin, while I wanted to make sure it got deep into the joint , I found out when I turned the boat over to do the other side that I had a lot of epoxy drip thru and actually glue the bulkheads to the hull. This added several hours of clean up and some damage chiseling the parts apart.
When I filled the wire holes, I used a putty knife and used a technique much like filling dry wall nail holes. I did not clean up too well and left spots that needed sanding later. When I filled nail holes in the inside and elsewhere, I used alcohol to wipe up the excess left by the putty knife. This eliminated a few hours or sanding.
Applying the fiberglass to the bottom of the boat went well. I used the suggested amount of epoxy and it spread out nicely. The inside was another story. I could not get the epoxy to spread out to the edges. I poured it into the middle as suggested in the manual. I had to use extra epoxy to wet out all the glass. In fact after I got done I added up the epoxy used and found I had used twice the amount suggested. It seemed to be OK, so I went off to bed expecting good results.
I came down an hour later and found bubbles and many areas where the glass cloth had lifted off the surface of the wood. I worked for an hour to try and smooth it out. I finally realized It was hopeless and removed the glass from the wood. I rolled and tipped the epoxy to reduce sanding time and had a stiff drink.
Here lies $30 worth of glass cloth and a lot of epoxy.
Oh Well still better than being out in the snow!
It worked out in the end. I found a local source for glass cloth and this time I poured the epoxy around the edges of the inside and worked it towards the middle. Sometimes common sense is better than directions.
I found a better solution to removing the wire than using a lighter. My thumb got raw flicking by Bic to heat up the wires to remove them. I used my heat gun which worked very well and cut the time by 50%. I found I could heat the wire with one hand and pull with a pair of pliers in the other. A propane torch would work too, but a heat gun is safer.
The transoms were a challenge. The stern was a dream, but the bow was harder. I would advise making an effort to attach the forward transom even with the shortest panel. I wired it too far forward and had a gap to make up for. Strangely this mistake saved me from another one later on. I did not have my glasses on and mistook a 6 for an 8 and put the forward bulkhead two inched too far forward. As I had put the transom too far forward, it worked out. I would rather be lucky than good!
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